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View Full Version : Travis' Never ending '87 Supra Build.


TravisD
08-21-2011, 01:49 AM
Figured it's about time I made one of these, I've had the car for well over a year now. Originally purchased in summer of 2010, I drove it for about two weeks and then tore it apart and started fixing/modifying it.

Here's the car when I originally got it -

http://i18.photobucket.com/albums/b117/VeilSideZX/100_0539.jpg

The body on the car is what really motivated me to buy it, one of the cleanest MkIII's I've ever come across. It was in roughish shape mechanically, but after $2700 of steering and suspension work, new exhaust gasket and helicoiled studs, it was well on its way.

Shortly after that work was done, I put a boost controller in and tried to run 12psi on the stock ct26. I blew apart almost every single intercooler pipe and then the turbo started blowing oil, the car needed some serious work, so I purchased an HKS intercooler kit, and got ready to install a gt35r.

Here's the manifold with an adapter plate small enough to finally let my upper ic pipe clear -

http://i18.photobucket.com/albums/b117/VeilSideZX/297817_10150759989065398_594565397_20079543_175967 5_n.jpg

And here's what the turbo looked like mocked up in the car -

http://i18.photobucket.com/albums/b117/VeilSideZX/307211_10150759988890398_594565397_20079542_608599 8_n.jpg

After I got the car to this point, I realized there was absolutely zero chance of the oil lines clearing so in an effort to actually drive the car at some point this year, I opted for a different, more manageable turbo. This was a really big piss off because I was really looking forward to the gt35r but hey! I also had a spare 57 trim ct26 in the shop that needed a rebuild, so I dropped it off at Alamo industries, and two days later I wound up with a brand new, slick as hell looking 60-1 upgrade in the turbo!

Turbo before rebuild -

http://i18.photobucket.com/albums/b117/VeilSideZX/IMG-20110501-00035.jpg

Turbo after rebuild, side by side to a stock ct26 -

http://i18.photobucket.com/albums/b117/VeilSideZX/229732_10150744744015398_594565397_19892302_285920 1_n.jpg

RC 550's and a lex afm were installed next -

http://i18.photobucket.com/albums/b117/VeilSideZX/226374_10150579423845398_594565397_18172403_707992 8_n.jpg

And shortly after I started on the HKS intercooler kit, this should have went nice and smooth but I had no instructions, and was missing all the brackets from the kit. After playing jigsaw puzzle for a good while, and receiving a helpful email from mstgeer on supramania (thanks again!) my dad and I fabbed up some brackets and mounted the intercooler -

I forgot to take a pic after, but the custom brackets also allowed it to sit nice and straight, instead of on a weird angle like most of the HKS kits I've seen.

http://i18.photobucket.com/albums/b117/VeilSideZX/306086_10150759988320398_594565397_20079538_193433 8_n-1.jpg

Also prior to installing the IC, I found a TON of rust behind the bumper from an exploded battery. After a good while of grinding and sanding and painting I fixed it up and got it looking fresh again

Ended up painting the entire thing flat black, but forgot a pic again -

http://i18.photobucket.com/albums/b117/VeilSideZX/301908_10150759989170398_594565397_20079545_279222 1_n.jpg

Finally after all this BS, all the little things were ready to go in, this included an Apexi SAFC II, Innovate wideband, and a few other little goodies to get things running a bit more proper. A year and a half later, the car is good to go!

Fresh after a quick wash and wax -

http://i18.photobucket.com/albums/b117/VeilSideZX/316352_10150759988205398_594565397_20079537_661645 0_n.jpg

Finally got the chance to take the car down to the track last night, running 15psi of boost with my afr's around 10.5 I pulled a 13.66 for my first pass. I was super disappointed with that run, but hey, first time EVER launching the car and my 60ft was a 2.490. Definitely need to invest in some slicks! After that I had a really good launch, and felt really good going down the track against a 11' Camaro SS, unfortunately when I went to pick up my slip the guy told me the time machine broke so they had no idea what I ran. FML. I also happened to notice my downshifts were feeling pretty damn weird and the car overheated, so that put a quick end to my racing fun. After getting the car home I found a hairline crack in my radiator, and a jacked up carrier bearing on the driveshaft. Just ordered the new bearing from Toyota and it came with a free keychain, lol thanks again Jeff, and now I guess I need to find a solution for my rad issue.... So the car is parked again for a bit till I get everything sorted out, but I also just ordered a Blitz Nur Spec exhaust, radiator hardpipe kit, and a Shine front lip, can't wait till all that arrives! I guess in the meantime here's a complete mod list of the car and a few more pics, sorry if I rambled a bit but hey! This is my timeline I guess for the car and the only real way I'll remember everything that's gone on. Enjoy!

'87 Supra Turbo Targa

Rebuilt JDM 7mgte from a '92
Ceramic coated pistons
Arp head, rod, and main bolts
HKS MHG
Ported and Polished head
HKS Turbo Exhaust
HKS Downpipe
HKS Intake
Lexus AFM
60-1 Upgraded CT26
RC 550cc Injectors
MKIV TT Fuel Pump
Turbo XS RFL
HKS FMIC
Cusco Strut Bar
Eibach Springs
Tokico Shocks
Apexi SAFC II
HKS Turbo Timer
Innovate Wideband
Autometer Gauges
Greddy Profec B
Short Shift Kit
17" Enkei RPO2's

TravisD
08-21-2011, 01:50 AM
http://i18.photobucket.com/albums/b117/VeilSideZX/FrontLeftFogsonly.jpg
http://i18.photobucket.com/albums/b117/VeilSideZX/100_0614.jpg
http://i18.photobucket.com/albums/b117/VeilSideZX/DSC00028.jpg
http://i18.photobucket.com/albums/b117/VeilSideZX/100_0587.jpg

TravisD
08-21-2011, 01:52 AM
And here's my run with no time....
http://i18.photobucket.com/albums/b117/VeilSideZX/th_DSCN1104.jpg (http://s18.photobucket.com/albums/b117/VeilSideZX/?action=view&current=DSCN1104.mp4)

Mr Malaka
08-21-2011, 11:00 AM
Looks really nice. Previous owner did the engine rebuild, or was that you?

TravisD
08-21-2011, 11:07 AM
The previous owner did the rebuild, as far as I know the car had it's original motor rebuilt by Raymond at Silverstone, then the car was sold and ~15,000km after that the motor blew up again and the jdm 7mgte was swapped in and rebuilt by Raymond again. This motor has ~10,000km on the rebuild, crossing my fingers that it lasts.. burns a bit of oil and leaks pretty bad, but I'm hoping that's just valve stem seals and the centre valve cover gasket. Did a compression test on it yesterday and it was 149, 150, 143, 148, 150, 149 I think..

Mr Malaka
08-21-2011, 01:56 PM
Yeah I'd be crossing my fingers...don't know Raymond personally, but after one of his engines blowing that soon, and now leaks plus burning oil on this one I'd be a little concerned.

TravisD
08-21-2011, 05:11 PM
I honestly haven't heard a lot of good things about him... I kind of want to take the car up the Edmonton and tell him to fix it, because his second motor for the car is turning shitty, and the turbo he built for it blew up in less than 10,000km as well - that was the 57 trim I just had rebuilt again, and Alamo said it looked like shit on the inside. I have $15,000 in receipts from his shop for the motor, it's pretty ridiculous it's running the way it is right now!